A-004
Encyclopedia
A-004 was the sixth and final test of the Apollo launch escape vehicle and the first flight of a Block I production-type spacecraft.
conditions in which the command module structure was loaded to the design limit.
The launch vehicle was the fifth and final Little Joe II
flown. The propulsion system consisted of four Algol and five Recruit rocket motors. The attitude control system was similar to the one used on mission A-003 except that the reaction control system was deleted and the vehicle was provided with the capability of responding to a radio-transmitted pitch up command. The
pitch up maneuver was required to help initiate tumbling of the launch vehicle. The spacecraft for this mission consisted of a modified Block I command and service module boilerplate, BP-2, and a modified Block I launch escape system
(airframe 002). The center of gravity and thrust vector were changed to assure that power-on tumbling would be attained after abort initiation. The earth landing system was essentially the same as that used during Pad Abort Test 2.
All systems performed satisfactorily, and the dynamic loads and structural response values were within the design limits and predicted values. Although a structural loading value of primary interest was not achieved (local differential pressure between the interior and exterior of the command module wall), all test objectives were satisfied.
Objectives
Mission A-004 was unmanned and was conducted to demonstrate that (1) the launch escape vehicle would satisfactorily orient and stabilize itself in the proper attitude after being subjected to a high rate of tumbling during the powered phase of an abort and (2) the escape vehicle would maintain its structural integrity under testconditions in which the command module structure was loaded to the design limit.
The launch vehicle was the fifth and final Little Joe II
Little Joe II
Little Joe II was an American space launch vehicle used for five unmanned tests of the launch escape system and to verify the performance of the command module parachutes for the Apollo spacecraft from 1963–66...
flown. The propulsion system consisted of four Algol and five Recruit rocket motors. The attitude control system was similar to the one used on mission A-003 except that the reaction control system was deleted and the vehicle was provided with the capability of responding to a radio-transmitted pitch up command. The
pitch up maneuver was required to help initiate tumbling of the launch vehicle. The spacecraft for this mission consisted of a modified Block I command and service module boilerplate, BP-2, and a modified Block I launch escape system
Launch escape system
A Launch Escape System is a top-mounted rocket connected to the crew module of a crewed spacecraft and used to quickly separate the crew module from the rest of the rocket in case of emergency. Since the escape rockets are above the crew module, an LES typically uses separate nozzles which are...
(airframe 002). The center of gravity and thrust vector were changed to assure that power-on tumbling would be attained after abort initiation. The earth landing system was essentially the same as that used during Pad Abort Test 2.
Flight
The vehicle was launched on January 20, 1966, at 08:17:01 a.m. MST (15:17:01 UTC) after several postponements due to technical difficulties and adverse weather conditions. The pitchup maneuver was commanded from the ground when telemetry showed that the desired altitude and velocity conditions had been reached. The planned abort was automatically initiated 2.9 seconds later. The launch escape vehicle tumbled immediately after abort initiation. Pitch and yaw rates reached peak values of 160 degrees per second, and roll rates reached a peak of minus 70 degrees per second. The launch escape system canard surfaces deployed at the proper time and stabilized the command module with the aft heat shield forward after the escape vehicle had tumbled about four times. Tower jettison and operation of the earth landing systems were normal, and the command module landed about 113,620 feet (34.6 km) from the launch pad after having reached a maximum altitude of 78,180 feet (23.8 km) above mean sea level.All systems performed satisfactorily, and the dynamic loads and structural response values were within the design limits and predicted values. Although a structural loading value of primary interest was not achieved (local differential pressure between the interior and exterior of the command module wall), all test objectives were satisfied.